Have been struggling with this engine for a while..... Long story short... It turns out the problem was the plug was gapped at .018 , and when I regapped it to .028 zooom zooom zooom..... I must have dropped the plug.....
I'm wondering if that's not what's wrong with mine. Having 4-stroking problems. It's still in the break-in stage. Only a week old with around 20 miles on it.
I got to thinking about how I always eyeball my plug gaps and decided to check all my junk to see where my eye was.
Four engines, four plugs between .020 and .030!
Guess doing it long enough gives decent repeatability.
(I do still have a plug gapper though I hardly ever use it.)
Well, I gapped my plug out to .025 and it seems to run a little better now. Still have the stock Chinese junker. NGK next week. The 4-stroking is not as bad now. A bit more power than before. Not a whole lot, but noticeable. Again, she's still in the break-in stage. Time will tell.