bigcitybikes
New Member
also i think the cap on the spark is crappy would love to buy a replacement plug cover that actually clicks in!!! autozone didnt have one!



Had a chance to test the bike tonight, and she ran much better with the jet drilled out. Night and day difference! So here is where I am currently: The jet was drilled out with a #69 bit. The needle is in the 4th notch down and the air mix screw is 2.5 turns out. I'm still on break in mix @24:1. Hope this helps all who are struggling with this carb. Don't give up on it. Not a bad carb if you can get it tuned. I still feel like it starves very slightly @ WOT, may go to #68 bit but will wait and finish break-in first before doing that. My observations on this carb are: the carb seal at the intake must be done using sealant or an air leak is likely. The float may not be set correctly at the factory and lastly the carb may be under-jetted as mine was. I'll continue to mess with it and tune it until I break it and am forced to buy another one!LOL.
would I stop that>
