Cylon
Member
Hey all I was riding my bike to work yesterday and the engine was backfiring a ton almost like it was four stroking but in fact it was backfiring. So I changed the plug almost made it to work then the engine shut down and failed to restart.
So far I've pulled the whole top end off nothing wrong with it, in fact it looks amazing. I did some more porting and filed down the intake piston skirt.
Next I checked the magneto magnet and it seemed Okay. I pulled it off anyways just too look at the woodruff key and that was fine maybe a little loose.
Tonight I'm going to put the engine back together with new rings and try it out if that fails I'll just buy a new cdl because my magneto is fine.
So far I've pulled the whole top end off nothing wrong with it, in fact it looks amazing. I did some more porting and filed down the intake piston skirt.
Next I checked the magneto magnet and it seemed Okay. I pulled it off anyways just too look at the woodruff key and that was fine maybe a little loose.
Tonight I'm going to put the engine back together with new rings and try it out if that fails I'll just buy a new cdl because my magneto is fine.